Integrated dry NO sub x /SO sub 2 emissions control system

The DSI system design is approximately eighty percent completed. About eighty percent of the materials have been purchased for erection and setup of the DSI system. Most of the equipment and supply purchases have been made for the DCS. The Unit 4 outage started March 20, 1992 for the installation of...

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Other Authors: United States. Department of Energy.
Format: Report
Language:English
Published: Public Service Co. of Colorado, Denver, CO (United States) 1992
Subjects:
Online Access:https://doi.org/10.2172/7282016
https://digital.library.unt.edu/ark:/67531/metadc1451118/
_version_ 1821489677484425216
author2 United States. Department of Energy.
collection University of North Texas: UNT Digital Library
description The DSI system design is approximately eighty percent completed. About eighty percent of the materials have been purchased for erection and setup of the DSI system. Most of the equipment and supply purchases have been made for the DCS. The Unit 4 outage started March 20, 1992 for the installation of the remaining project equipment. overall field construction activities continued on the flyash, boiler, dry sorbent injection and humidification systems. Noell performed startup and testing activities for the urea injection system. FERCO completed baseline urea injection tests March 6, 1992. Preliminary analyses were reviewed at a project review meeting on March 11, 1992. The HVAC platform and duct work for the DCS was installed. B W mobilized on site. Demolition and construction activities began to support the future installation of the low NO, burners and ports. CSM completed the batch reactor vessel. The sorbent and flyash silos were erected for the DSI system. The humidification building was erected and piping for the fly ash silo started.
format Report
genre Carbonic acid
genre_facet Carbonic acid
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institution Open Polar
language English
op_collection_id ftunivnotexas
op_doi https://doi.org/10.2172/7282016
op_relation other: DE92019717
rep-no: DOE/PC/90550-T6
grantno: FC22-91PC90550
doi:10.2172/7282016
osti: 7282016
https://digital.library.unt.edu/ark:/67531/metadc1451118/
ark: ark:/67531/metadc1451118
publishDate 1992
publisher Public Service Co. of Colorado, Denver, CO (United States)
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spelling ftunivnotexas:info:ark/67531/metadc1451118 2025-01-16T21:28:13+00:00 Integrated dry NO sub x /SO sub 2 emissions control system United States. Department of Energy. 1992-05-15 13 pages Text https://doi.org/10.2172/7282016 https://digital.library.unt.edu/ark:/67531/metadc1451118/ English eng Public Service Co. of Colorado, Denver, CO (United States) other: DE92019717 rep-no: DOE/PC/90550-T6 grantno: FC22-91PC90550 doi:10.2172/7282016 osti: 7282016 https://digital.library.unt.edu/ark:/67531/metadc1451118/ ark: ark:/67531/metadc1451118 Urea Chemical Reactions Wastes 200202* -- Fossil-Fueled Power Plants-- Waste Management-- Noxious Gas & Particulate Emissions Desulfurization Organic Compounds Progress Report Document Types Amides Air Pollution Control Power Plants Gaseous Wastes Flue Gas 20 Fossil-Fueled Power Plants Sorbent Injection Processes Burners Combined Soxnox Processes Control Carbonic Acid Derivatives Organic Nitrogen Compounds Denitrification Fossil-Fuel Power Plants Thermal Power Plants Pollution Control Report 1992 ftunivnotexas https://doi.org/10.2172/7282016 2019-05-04T22:09:03Z The DSI system design is approximately eighty percent completed. About eighty percent of the materials have been purchased for erection and setup of the DSI system. Most of the equipment and supply purchases have been made for the DCS. The Unit 4 outage started March 20, 1992 for the installation of the remaining project equipment. overall field construction activities continued on the flyash, boiler, dry sorbent injection and humidification systems. Noell performed startup and testing activities for the urea injection system. FERCO completed baseline urea injection tests March 6, 1992. Preliminary analyses were reviewed at a project review meeting on March 11, 1992. The HVAC platform and duct work for the DCS was installed. B W mobilized on site. Demolition and construction activities began to support the future installation of the low NO, burners and ports. CSM completed the batch reactor vessel. The sorbent and flyash silos were erected for the DSI system. The humidification building was erected and piping for the fly ash silo started. Report Carbonic acid University of North Texas: UNT Digital Library
spellingShingle Urea
Chemical Reactions
Wastes 200202* -- Fossil-Fueled Power Plants-- Waste Management-- Noxious Gas & Particulate Emissions
Desulfurization
Organic Compounds
Progress Report
Document Types
Amides
Air Pollution Control
Power Plants
Gaseous Wastes
Flue Gas
20 Fossil-Fueled Power Plants
Sorbent Injection Processes
Burners
Combined Soxnox Processes
Control
Carbonic Acid Derivatives
Organic Nitrogen Compounds
Denitrification
Fossil-Fuel Power Plants
Thermal Power Plants
Pollution Control
Integrated dry NO sub x /SO sub 2 emissions control system
title Integrated dry NO sub x /SO sub 2 emissions control system
title_full Integrated dry NO sub x /SO sub 2 emissions control system
title_fullStr Integrated dry NO sub x /SO sub 2 emissions control system
title_full_unstemmed Integrated dry NO sub x /SO sub 2 emissions control system
title_short Integrated dry NO sub x /SO sub 2 emissions control system
title_sort integrated dry no sub x /so sub 2 emissions control system
topic Urea
Chemical Reactions
Wastes 200202* -- Fossil-Fueled Power Plants-- Waste Management-- Noxious Gas & Particulate Emissions
Desulfurization
Organic Compounds
Progress Report
Document Types
Amides
Air Pollution Control
Power Plants
Gaseous Wastes
Flue Gas
20 Fossil-Fueled Power Plants
Sorbent Injection Processes
Burners
Combined Soxnox Processes
Control
Carbonic Acid Derivatives
Organic Nitrogen Compounds
Denitrification
Fossil-Fuel Power Plants
Thermal Power Plants
Pollution Control
topic_facet Urea
Chemical Reactions
Wastes 200202* -- Fossil-Fueled Power Plants-- Waste Management-- Noxious Gas & Particulate Emissions
Desulfurization
Organic Compounds
Progress Report
Document Types
Amides
Air Pollution Control
Power Plants
Gaseous Wastes
Flue Gas
20 Fossil-Fueled Power Plants
Sorbent Injection Processes
Burners
Combined Soxnox Processes
Control
Carbonic Acid Derivatives
Organic Nitrogen Compounds
Denitrification
Fossil-Fuel Power Plants
Thermal Power Plants
Pollution Control
url https://doi.org/10.2172/7282016
https://digital.library.unt.edu/ark:/67531/metadc1451118/